So the customer bought a sleeve to fit into the block, and I bored it out to match the sleeve, but left it at the outside diameter of the sleeve -.002" so there'd be an interference fit.
To see a couple of short video clips of the boring bar in action please go to either of the following links;
https://youtu.be/kzeWYh-gjSA
to see the boring bar reboring the Elan engine. In the clip you can see that the Elan was parked on quite a slope, and the engine was at quite a difficult angle to work on.
https://youtu.be/LBX28eOEZHE
to see the boring bar reboring a Toyota Supra engine. In this clip you can see that the Toyota engine was much more horizontal, and therefore easier to work on.
With the block taken out to the outside diameter of the sleeve, -.002", the customer cut the sleeve to about 1/4" too long, then froze it in his freezer. After which we applied liberal amounts of Loctite 648 to glue the sleeve into position.
I also deliberately left a small ledge at the bottom of the bore to prevent the sleeve from slipping downwards.
We then set about fitting the sleeve without the aid of a 10 ton hydraulic press, which is what would normally be used in this situation. However, all we had was a 2lb lump hammer and a block of wood. So that had to suffice.
I held the wood across the top of the sleeve and the customer hit it with the hammer many times, till the wood split. He then cut another block of wood, but that also split almost immediately, so then he found a flat steel bar, and we used that across the top of the sleeve to hammer it in.
As you can see in the previous picture, the metal bar did some damage to the top of the sleeve, but because the customer had deliberately cut it long, once inserted it was still above the level of the block, so I was able to cut it back using the boring bar cutter.
NOTE: Needless to say, I don't recommend anyone fit a sleeve with the engine still in the chassis, and without the proper hydraulic press, but surprisingly we did manage to do just that, and it all went without a hitch.
I cut the excess height off the sleeve by setting the cutter to a size much larger than the sleeve, and carefully lowering the cutter till the flat bottom edge of the cutting tip cut the top off the sleeve.
I left the sleeve a few thou above the surface of the block and then removed the bar so that the sleeve could be slowly and carefully filed back flush.
With the sleeve now safely in position and cut to length I bored it out to standard size, but the customer had already purchased a set of pistons at +.020" oversize, so all four cylinders had to be bored out to that.
The rest of the job went as per normal, with me boring out the four cylinders to +.019", then honing them the last .001" to the finished size.
The picture above shows the four cylinders at their finished size and with their cross hatch finish. The customer then has to clean all the metal dust away (he used a small vacuum to do most of the work), lubricate everything, and reassemble.
Job Done!
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